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This article considers the utilisation of modern image processing and enhancement to determine the impact of the catastrophic failure of Cryogenic Oxygen Tank 2, and it's subsequent impact on Bay 4 and critical systems on Apollo 13. The analysis also aims to aid visualisation and identify key components of the damaged Service Module.
Details of the original photographic analysis which formed a significant part of the 1970 investigation can be found in Apollo 13 document collection with particular reference to the following documents: //
Only around half a second separated the first vibrations detected in the accelerometers (caused by changing pressures in oxygen tank 2) and rapid pressure increase in Bay 4, leading to panel blow out. A calculated 60,000-pound force was effected on the CSM and 1.17g was recorded in the X-axis as the panel blew out and contacted the High Gain Antenna, although the actual total attitude change was small.
The shock loads closed several reaction control propellant isolation valves and the reactant valves in the fuel cell oxygen system leading to the loss of electrical power from fuel cells 1 and 3. The oxygen tank 2 feedline or pressure transducer wiring / plumbing was also severed leading to a zero reading on tank 2.
Damage to the adjacent oxygen tank 1 lead to a leak, and this venting oxygen caused attitude changes necessitating stabilisation from the attitude control system. However, some thrusters were assigned to main bus B which received electrical power from the now dead fuel cell 3 and as such were not functioning.
For the next 1.5 hours there were confusing firings of the attitude control thrusters. Lovell struggled to regain correct attitude manually, only re-assigning the thrusters to main bus A allowed Lovell to eventually regain control.